1986 Chevy 1 Ton 5 Speed Manual Transmission Swap - 4Wheel & Off-Road Magazine

1986 Chevy 1 Ton 5 Speed Manual Transmission Swap Fred Williams Brand Manager, Petersen’s 4Wheel & Off Road 1986 Chevy 1 Ton interior Photo 9268756

When you're building a truck to take off road, gearing is a pillar of performance. Low gearing for crawlingand turning big tires can't be beat, but if your truck also acts as a daily driver, then you may need both low-end gearing as well as high-speed overdrive options. We recently doubled our crawl ratio, took 25 percent off our high gear ratio, and gave our truck two more gears to play with by replacing the TH400 automatic and NP208 transfer case with an NV4500 five-speed manual and the new 3:1 LoMax 205 transfer case (see our complete LoMax story, "3:1 Low Gears for an NP205," Jan. '07). After swapping out the automatic transmission we also found more performance out of our underpowered V-8 diesel by eliminating the fluid coupler of the torque converter and replacing it with a direct-drive clutch system. Putting a manual trans behind an underpowered engine is a great way to wind a few more ponies from it whether it's a tired diesel or an anemic four-cylinder.

Our test mule for this swap is our '86 Chevy 1-ton known. The truck is an all-around workhorse...from a parts hauler to camping platform to highway cruiser. As much as we like the truck, the sparse interior and rattling diesel made for annoyingly loud road trips, and an overdrive would reduce the engine revs as well as giving us a mileage benefit. Off road we've been very happy with our automatic, but sometimes felt that having the ability to drop the clutch for an aggressive holeshot launch would have given us that extra momentum to get moving through a deep mud hole or up a steep climb we couldn't just crawl. By hooking up with the crew from Gear Tech Heavy Duty we quickly had everything needed to swap our truck from three speeds to five and from two pedals to three. Gear Tech HD specializes in drivetrain parts from transmissions to axles, and its manual transmission swap kit included all the bits so we had no need to go crawling around a junkyard hunting parts. This of course was helped by the fact that our model truck was originally offered with a manual, but never with the five-speed tranny so some innovation was required. As this goes to press the project is being buttoned up, so head over to our Web site (www.4wheeloffroad.com) for our driving impressions and the mileage results by going to the "Man Plan."

PhotosView Slideshow In order to make our automatic-to-manual swap quick and easy we dumped all the parts in the bed and headed to Randy's Off-Road in Azusa, California. Randy's bread and butter is building fullsize trucks for playing in the mud, and this swap has been done more than once on Randy's outdoor lift. Yes, this whole swap was done outside-in December, and in weather warm enough to wear shorts. Southern California may not be the best place to live, but it has its benefits. Gear Tech Heavy Duty can supply just the transmission or a complete conversion kit depending on your application. Since our truck's body style was available with a manual transmission option, Gear Tech supplied us with a set of refurbished brake and clutch pedals along with a clutch, a flywheel, a throwout bearing, a pilot bushing, aftermarket bellhousing input shaft and tailhousing adapters, and the NV4500 five-speed transmission. The NV4500 transmission (foreground) we used has a first-gear ratio of 5.61:1, which offers us great creeping-around gearing, and a 0.74:1 overdrive. The entire length of the transmission and bellhousing is 27 1/2 inches, just slightly longer than our TH400 at 27 1/4 inches (background). This transmission has been found behind big-block gas engines and heavy-duty diesels, so we feel that our relatively ho-hum 6.2 turbodiesel should in no way be taxing it. After removing the TH400/NP208 original drivetrain we installed a flywheel and clutch. This will hopefully be our only maintenance item in the future for the trans and transfer case. Also note the hard lines hanging down that ran from our automatic to the tranny cooler built into our radiator. They will be removed and the cooler openings looped back into themselves with a vent to release the pressure that builds up in the system. Next we assembled the NV4500 with the bellhousing and throwout bearing. The kit came with a plastic throwout bearing which cracked during assembly, so we replaced it with a sturdy steel unit. The clutch fork has a small circle clip that hooks over the pivot ball in the bellhousing. Ours required some tweaking of the clip, and a few choice words before it snapped into place. As we installed the transmission into the truck we hit a glitch with the diesel starter. The nose cone is larger than those found on the gas starters and unfortunately it wouldn't fit into the aftermarket bellhousing. 1986 Chevy 1 Ton grind Bellhousing Photo 9268867

Rather than swap in a lesser starter, Randy took some time with a grinder to carve out the aluminum bellhousing. We're sure we could have spent hours at the local parts yard searching for a diesel bellhousing, but by covering everything with rags and taking our time we soon had the clearance we needed.




1986 Chevy 1 Ton transfer Case Photo 9268774

In addition to the overdrive gearing of the NV4500, we also chose to install the new LoMax 205 transfer case from JB Conversions. By replacing the factory NP208 (background) with the 205 (foreground) we went from a 2.6:1 to 3.0:1 low range that resulted in a crawl ratio of 76.7:1 versus the previous 29.4:1 with the automatic. Furthermore we gained low range in two-wheel drive, went from an aluminum case to cast iron, and eliminated the transfer-case slip yoke. We may get some gear noise by replacing the chaindriven 208 with the big gears in the LoMax 205, but that is a sacrifice we are willing to make for the strength gain. Additionally, overall length is reduced from 18 1/2 (208) to 12 1/2 inches (205).

1986 Chevy 1 Ton cut Exhaust Photo 9268873

Our mockup with the transfer case found some more speed bumps. The exhaust from our Banks Turbo wanted to occupy the same position as the LoMax 205. Sawzall to the rescue. The factory crossmember and the front output got into a little dispute, and though we had already modified the crossmember with an additional 1/4-inch plate to raise the tail of the transmission, it still wasn't going to work.


PhotosView Slideshow Our solution came in the form of a crossmember out of a mid-'80s Chevy with a 700R4/208 combo. Since the tailhousing of the NV4500 had been slotted to clear the LoMax 205 shift rails, there is only one clocking angle for the 205. Luckily this factory crossmember drops down on the passenger side to clear the front driveshaft. We did need to grind a bit off the back of the crossmember to clear the LoMax 205, and we installed the crossmember inside the framerails which will require complete disassembly for removal in the future, but it was still easier than fabricating a completely new piece. Moreover the crossmember hangs down lower than the 205, and allowed us to use the original skidplate with a little massaging. From the front side you can see how the Off Road Design twin-stick shifters attach. These shifters and the modified shift rails of the LoMax 205 allow for two-wheel drive in high and low range from either the front or rear axle as well as high and low range in four-wheel drive. In addition, the shifter comes right up through the original hole in the floor for the 208 shift lever. We did need to cut a hole for the shift tower on the NV4500. This was done by first trimming the vinyl floor mat and insulation in as small an opening as possible. Then by tracing the shift tower onto the steel floor directly above the trans we were able to cleanly cut out the opening. We will eventually find a thick rubber shift boot to keep heat, fumes, and noise out of the cab. After taking careful measurements we ordered up a new pair of driveshafts from Denny's Driveshafts in New York. Our front driveshaft was shorter and no longer uses a constant velocity joint. We determined that dual 1350 U-joints would be sufficient in strength and still offer us enough angle. Plus since we will rarely be driving at highway speeds at full angle, the front shaft should be fine without a CV. Out back we also replaced the shaft with a new Denny's unit. Again 1350 joints are employed and since the LoMax 205 has a solid yoke we had a slip spline built into the shaft. These shafts do not have as thick a wall as our dedicated rockcrawler's shafts, but since highway speeds will be more common than daily dirt with this truck, that was less of a priority. The 205 received a few quarts of Lucas Synthetic 75W90 gear oil, while the NV4500 requires the more expensive and less common Castrol Syntorque. We could only find the Syntorque at a GM dealer, though a Dodge dealer should also carry it since NV4500s were also found in Dodge trucks. The special lube is required for the synchros and bearings of the transmission, and since it's a dealer item they'll ask for both an arm and a leg as payment. These finned-aluminum PTO covers help dissipate heat which can build up after long climbs or when towing. (Note-it is not a good idea to tow with the NV4500 in the overdrive gear.) As an added bonus there is a temperature sending unit in the cover and a temp gauge in the Gear Tech kit to help keep track of the trans. Luckily the factory brake pedal and new clutch/brake pedals simply bolt in and out with no extra holes required. However it did require complete removal of the steering column, which presents a great time to upgrade to a tilt and manual trans unit if you please. We chose neither. We were required to drill some holes for the hydraulic-clutch master cylinder, but careful inspection revealed some embossed marks on the firewall where a factory unit would have gone. We double-checked that they would work, and then drilled them out before bolting the master cylinder in with the new pedals. The bellhousing mount for our slave cylinder needed to be slightly modified, but we assume this was again due to the diesel engine; possibly using a thicker flywheel then the bracket was designed for. In order to keep the slave from engaging the clutch when simply bolted on, we had to shorten the pushrod about an inch. The final step was to plumb the clutch and mount the reservoir. We found a factory GM unit that worked perfectly. All that's left is to repair the exhaust and hit the road. Check out our Web site (www.4wheeloffroad.com) for our driving reviews of going from the automatic to the five-speed manual as well as notes on mileage gains we found by being able to shift into Overdrive and let the engine relax at highway speeds.